Austman
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- Sep 21, 2007
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was on the DPS-MEL sector of the inaugural JQi 787 MEL-DPS-MEL service yesterday. The first international flight of the new 787.
About an hour out of DPS we nearly diverted. I'd guess it would have been to DRW which was by then about as far away as DPS.
The 787 was making a huge noise (like a hair dryer/vacuum cleaner) with vibration about 2 thirds back in the Y cabin. It was coming from under the floor. If you stood in the area your whole body vibrated!
The captain inspected the issue and kept the pax well informed. It was announced that it was not safety related. The captain said has was in a 3-way conference call with JQ maintenance and Boeing. After again being told it was a non-safety related issue, the captain announced that he was more concerned with passenger comfort - the noise and vibration the the area were pretty bad. But the plane was far from full, so pax could be relocated away from the noisiest part. Apparently the most affect pax were consulted and stated that they preferred to continue to MEL which we did.
So it was quite nicely handled by the crew. I think it would have been a different result if the plane had been full.
I'm guessing it could have been an air-conditioning unit?
Unless it can be fixed today, I doubt if MEL-DPS will be operated by a 787 tonight.
About an hour out of DPS we nearly diverted. I'd guess it would have been to DRW which was by then about as far away as DPS.
The 787 was making a huge noise (like a hair dryer/vacuum cleaner) with vibration about 2 thirds back in the Y cabin. It was coming from under the floor. If you stood in the area your whole body vibrated!
The captain inspected the issue and kept the pax well informed. It was announced that it was not safety related. The captain said has was in a 3-way conference call with JQ maintenance and Boeing. After again being told it was a non-safety related issue, the captain announced that he was more concerned with passenger comfort - the noise and vibration the the area were pretty bad. But the plane was far from full, so pax could be relocated away from the noisiest part. Apparently the most affect pax were consulted and stated that they preferred to continue to MEL which we did.
So it was quite nicely handled by the crew. I think it would have been a different result if the plane had been full.
I'm guessing it could have been an air-conditioning unit?
Unless it can be fixed today, I doubt if MEL-DPS will be operated by a 787 tonight.